- Grab outside, attempt to spin (failed...)
The tight position of the bolt didn't give me enough room to grab it by the top and spin. If there wasn't so much other stuff in the way, this might have worked. - Screw extractor (failed...) I happen to have a set of screw extractors. They work by drilling a pilot hole and using another bit with reverse threading. When run in reverse to remove the screw, the bit digs into the metal, providing enough friction to wind the fastener out. The hardness of the metal used for this screw made it impossible for the reverse head to grab into the metal. I tried several different sizes, all with the same result.
- Decapitate, wind out remaining stem of screw (worked! jk, this failed too)
This is accomplished by running a drill bit through the center of the head, making a hole larger than the stem of the screw. When the drill reaches the stem, the head will have nothing fixing it to the stem and the remaining screw can be wound out once the part has been removed. The hardness of the faster made this slow going, to the point where the metal screw was being polished more than cut. - Cut head to fit slotted screw driver (victory!)
Used flat-head at 10 and 4
Should have done this from the start. Cut a slot on a radius line in the head of the fastener, use slotted screwdriver to remove. I didn't have an easy way to reach the bolt in question, but I did have a Dremel, I just needed the right cutting tool. The part wasn't accessible with a cut-off ring, but I could reach it with a plunge cut bit. Such a thing exists for Dremel tools, even rated to cut hardened metal: the 9903 Tungsten Carbide Cutter. At high speed, the bit chewed thought the metal no problem. With enough material cut away to fit a large screwdriver, I was able to get a twist on the bolt and break it free. Obviously, this method sacrificed the fastener, I'll need to get an approximate replacement at the hardware store.
So, it was dirty...
Something was leaking, so dirty |
Broken Transmission Cooling Lines
When I tried to remove the lines from the cover of the filter casing, they wouldn't budge. I had trouble reaching them from the top of engine to pull upwards, so I struggled from the bottom and when the first line came out the second, after a light tug, snapped. Or maybe not. Considering the amount of oil around the part, something was leaking and it wouldn't surprise me if this was in some nearly broken state at the start. At least my theory assuaged me as I went about searching for a new transmission cooling line.Finding the Part, found a new vendor
Amazon and RockAuto didn't stock this part, so I looked at the official Ford parts site ($107, next day availability) to get the part number and they searched to see if I could save a buck or two. I found the part at Tasca Auto parts for about $75 + $8 shipping. I saved a few dollars because I could afford to wait a few days. At Tasca I was completely surprised by the service: I sent some email to double-check if I was ordering the right part and somebody got back quickly asking for the VIN for verification and then replied with the correct part number I needed to order. I would have ordered the wrong part without checking with the vendor, so I'm glad I did. I'm guessing the customer service department at Tasca saves a huge amount in re-stocking costs by making it easy to verify fitment by VIN.Extraction...
Looking at the part, the break occurred in the groove accommodating the o-ring. This part of the pipe is thinner and thus weaker, and the odd insertion angle made removing this tube difficult. When we get the new part, I'll have to be extra careful when inserting it into the filter housing cover.
The Filter
Part of the old filter was stuck in housing |
Note larger opening on filter, at first I thought I had the wrong filter. |
Just so dirty... |
Not really sure why the old part has oxidizing |
Installing the Filter
I put some clean transmission fluid around the filter's o-ring and it popped right into place. I then put some new fluid on that rubber coated pipe thing and the o-ring on the cover and tried to seat the part. That didn't work, it just wobbled and I was worried I would damage the small tube part, so I replaced the T-40 screws one 10mm bolt and tightened them round-robin until they were nice and snug. I also did my best to clear away the gunk where the filter caps meets the transmission; I didn't want to get any contaminates into the transmission, so I did my best with a shop rag and very little de-greaser.
Next post, I'll cover replacing the broken line and putting things back together.
Next post, I'll cover replacing the broken line and putting things back together.
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